AAIU Reports

The following is a listing of Investigation Reports published by the Air Accident Investigation Unit concerning accidents and incidents that occurred within Ireland, including its airspace and territorial waters. This list will also include Investigations concerning Irish-registered and/or operated aircraft which were delegated to the AAIU by Foreign Accident Investigation Authorities in accordance with ICAO Annex 13. Reports may be sorted based on Occurrence Date or Publication Date using the Search Facility below.

Incident: BAe 146, G-TNTL, Dublin Airport, 12 Jan 1999: Report No 1999-006

May 28, 1999

SYNOPSIS

The aircraft had been positioned at Stand 67 at Dublin Airport.  The dolly struck the left hand undercarriage door and some damage was also evident to the lower part of the LH undercarriage body housing.  The force of the impact was felt by the captain who was in the cockpit at the time of impact.  He declared the aircraft unserviceable.

Accident: Jodel DR25, G-AWKP, Leperstown Dunmore East Waterford, 8 Jun 1998: Report No 1999-005

May 21, 1999

SYNOPSIS

The aircraft departed Little Gransden in the UK at 0740 hours on a Visual Flight Rules (VFR) flight to Waterford Airport in Ireland. The weather en route deteriorated, however, and the pilot elected to continue under Instrument Flight Rules (IFR). The pilot failed to establish on the ILS twice at his destination in Waterford Airport. During the course of the second go around, the pilot became visual and elected to land in a suitable field, as he considered he had insufficient fuel for additional approaches. 

The pilot landed the aircraft in a small and steeply uphill field. The aircraft came to a stop in a mud heap, just short of some farm out-buildings. There was no fire. All three occupants were uninjured. 

Accident: Sikorsky S61N, EI-MES, Dublin Port, 24 August 1998: Report No 1999-008

April 19, 1999

SYNOPSIS

EI-MES was performing a demonstration in Dublin Port, in association with the Tall Ships Event which was being held in Dublin. The demonstration consisted of dropping a team of nine swimmers of the Irish Naval Service Diving Section, from the helicopter into the River Liffey. When they jumped from the moving helicopter, the  swimmers suffered varying injuries. Two of the injured swimmers were hospitalised for more than 48 hours.

Incident: Boeing 737, EI-BXC, Cork Airport, 6 Jun 1998: Report No 1999-004

April 2, 1999

Synopsis

The AAIU was informed of this incident by Cork ATC at 0645 hrs on 6th. June 1998.
The aircraft which was on a holiday charter flight from Faro, Portugal, to Cork, landed on Runway 17 at Cork Airport. The weather conditions at the time were poor with mist, poor visibility and very low cloud.
The weather passed to the aircraft at 0505 hrs was:-
Wind 170/03,
Visibility 600 M, light rain and fog,
Cloud Scattered 100, Broken 200, Broken 600,
Temperature 12ºC
QNH 1004,
RVR 750 M, 1100 M.
During the landing roll a mechanical digger was observed by the crew to exit the runway on the right hand side approximately 250 feet in front of the aircraft. A van which was parked on the right hand side of the runway did not exit.
The aircraft was stopped short of the van using maximum reverse thrust and overriding the auto brake system to achieve greater braking than was available at the level 2 auto brake setting. It was also necessary for the aircraft to depart from the runway centreline.
 
 

Accident: Cyclone AX3, G-BUTC, Cushenstown New Ross Co Wexford, 16 May 1998: Report No 1999-003

March 24, 1999

SYNOPSIS

After a flight of one hours duration, and at about 800 feet while lining up with the runway to land, the aircraft went into an uncommanded left spiral dive from which the pilot recovered. He climbed back to 1,000 feet and, on reducing power, the aircraft again went into a left spiral dive from which he recovered. At this stage he had moved somewhat southwards away from his original intended landing area and, as he reduced power again the aircraft spiralled to the left and landed heavily in a nose down attitude in a field of barley.

Incident: Airbus A300, EI-TLL, Manchester International Airport, 17 July 1997: Report No 1999-002

March 15, 1999

This investigation was conducted by the Air Accidents Investigation Branch,UK, and the following report was originally published in AAIB Bulletin No.2/99 of February 1999.

 

Accident: Piper PA 32, G-ILTS, Warren’s airstrip Montague Gorey Co Wexford, 12 Nov 1996: Report No 1999-001

January 30, 1999

SYNOPSIS

During take-off from a grass airstrip near Gorey, Co Wexford, the aircraft did not become airborne until near the end of the runway, where it struck a barbed wire boundary fence, breaking two wooden poles in the process. The aircraft continued to fly with a high nose-up attitude for a further 300 metres before the pilot elected to carry out an emergency landing in an adjacent field. The field, which was cultivated and planted with small saplings, had furrows running at right angles to the direction of flight. After an initial heavy impact into the field, the main undercarriage was torn off and substantial damage was caused to the underside of the aircraft, before it finally came to rest. All five persons onboard the aircraft evacuated without injury. Time of impact was 0947 hours approximately. There was no fire. 

 

Incident: Model Aircraft, No reg, Dublin Airport, 7 Dec 1996: Report No 1998-017

December 20, 1998

Synopsis

The model was flying circuits at a registered aeromodel site in the Phoenix Park in Dublin.  After a take-off, which followed a normal circuit, command of the model was lost.  The model then flew off in a North-east direction.  When its fuel was exhausted, the model glided to earth, and landed on the new link taxi-way near the threshold of Runway 28 at Dublin Airport.

 

The report finds that the probable cause of the loss of command was the exhaustion of the receiver battery.

 

 

Accident: Bell 206 BII, Jet Ranger, EI-BYJ, North of Balbriggan, Dublin, 10 Nov 1997: Report No 1998-016

November 27, 1998

SYNOPSIS

On 10th. November 1997, the pilot, having completed a commercial flight earlier that morning, was requested by a member of the operators maintenance staff to carry out a local test flight on EI-BYJ, to confirm that the maximum and minimum autorotation RPM was set correctly, among other requirements.

His passenger, a qualified helicopter engineer, was on board to record various readings laid down in a document of eleven pages, entitled "Flight Test Schedule Ref. 125 Iss. 1 April 1991". The pilot and the engineer discussed the contents of this document in detail prior to take-off.

This particular flight was carried out prior to the commencement of the helicopters annual inspection, which was necessary for the renewal of its Certificate of Airworthiness (C of A). It was intended that any collective pitch control or cyclic control rigging adjustment would be carried out during this annual inspection. 

 

Accident: Robinson R22B, G-CLYV, Killary Harbour Galway, 14 Aug 1996: Report No 1998-015

November 12, 1998

SYNOPSIS

Aircraft suffered power failure and landed in 3 metres of sea water.           

 

 

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